辽东湾某油田大斜度井清除岩屑床技术的探讨
投稿时间:2013-11-29  修订日期:2013-12-09  点此下载全文
引用本文:和鹏飞.辽东湾某油田大斜度井清除岩屑床技术的探讨[J].钻探工程,2014,41(6):35-37.
HE Peng-fei. Discussion of Cuttings Bed Removing in Highly Deviated Well of an Oilfield in Liaodong Bay[J]. Drilling Engineering, 2014,41(6):35-37.
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作者单位E-mail
和鹏飞* 中海油能源发展股份有限公司工程技术分公司 hepf@cnooc.com.cn 
中文摘要:针对辽东湾某区块大斜度井出现的钻井液粘切高、起下钻困难、钻井液流变性不易控制的问题,从清理岩屑床入手,提出通过改善泥饼质量,保证井眼光滑、井壁稳定和保证钻屑携带的基础上,改变钻井液的流变性,使钻井液在钻铤处达到紊流,并及时使钻屑均匀分散在钻井液中,减少形成岩屑床的机会,达到清理岩屑床目的的新方法。该技术在该区块8口水垂比小于2的井上进行了施工,取得了理想的效果。
中文关键词:大斜度井  钻井液  流型  岩屑床
 
Discussion of Cuttings Bed Removing in Highly Deviated Well of an Oilfield in Liaodong Bay
Abstract:In view of the high viscosity of drilling fluid, difficult pipe tripping and hard control of drilling fluid rheology in a highly deviated well of a block in Liaodong Bay, a new technical method is put forward that starting from cuttings bed removing, on the basis of the improvement of mud cake quality to ensure a smooth borehole, stable borehole wall and effective cuttings carrying, the rheology of drilling fluid is controlled to be turbulence at the drill collar so as to the cuttings uniformly dispersing in the drilling fluid to reduce the formation of cuttings bed. In this block of Liaodong Bay, this technology is used in 8 wells with the horizontal distance and vertical distance ratio of less than 2, the ideal effects are obtained.
keywords:highly deviated well  drilling fluid  flow pattern  cuttings bed
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