顺北油气田二叠系火成岩钻井技术研究与应用
作者:
作者单位:

1.中国石化西北油田分公司石油工程技术研究院,新疆 乌鲁木齐 830011;2.中国石化缝洞型油藏提高采收率重点实验室,新疆 乌鲁木齐 830011;3.中国石化西北油田分公司石油工程监督中心,新疆 轮台 841600;4.中石化石油工程技术研究院有限公司,北京 102206

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中图分类号:

TE242;P634.5

基金项目:

中石化科研项目“塔里木盆地特深层钻完井工程技术示范”(编号:P21081-6)


Study and application of drilling technology for Permian igneous rocks in Shunbei Oil and Gas Field
Author:
Affiliation:

1.Engineering Technology Institute,Sinopec Northwest Oilfield Branch, Urumqi Xinjiang 830011, China;2.Key Laboratory of Enhanced Recovery for Fracture-cave Oil Reservoir, Sinopec, Urumqi Xinjiang 830011, China;3.Petroleum Engineering Supervision Center, Sinopec Northwest Oilfield Branch, Luntai Xinjiang 841600, China;4.Sinopec Research Institute of Petroleum Engineering Co., Ltd., Beijing 102206, China

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    摘要:

    塔里木盆地顺北区块二叠系火成岩地层厚度大、硬度高、裂缝发育、非均质性强,导致机械钻速低与堵漏耗时长,相比邻区平均钻井周期增加达1.5倍。近几年,通过持续强化钻井液堵漏技术与优选高效钻井工艺,漏失量与堵漏时间逐步缩短,钻井指标逐年提高。本文分析了影响堵漏时间长与机械钻速低的主控因素,提出堵漏浆中加入竹纤维、变形颗粒以改善堵漏工艺技术,明确了冲击工具的适用条件,优选攻击性与抗冲击性的PDC钻头,改进混合钻头结构以及配套大扭矩、长寿命螺杆等技术对策,提速降本成效显著,为加快顺北油气田的高效勘探开发提供了指导。

    Abstract:

    The Permian igneous rocks formation in Shunbei Block of Tarim Basin has the characteristics of large thickness, high hardness, developed fractures and strong heterogeneity, which leads to low ROP and long plugging time. the average drilling cycle increases by 1.5 times compared with the adjacent areas. In recent years, through continuous strengthening the drilling fluid plugging technology and the optimization of high-efficiency drilling technology, the leakage and plugging time have been gradually shortened, and the drilling index has been increased year by year. In this paper, the main controlling factors affecting the long plugging time and low penetration rate are analyzed, and the plugging technology is improved by adding bamboo fiber and deformed particles into the plugging slurry. The applicable conditions of the impact tool are clarified, and the PDC bit with aggressiveness and impact resistance is optimized. Technical countermeasures such as improving the structure of the mixed bit and supporting the high torque and long life screw have achieved remarkable results in increasing drilling speed and reducing cost, which provides guidance for accelerating the efficient exploration and development of Shunbei Oil and Gas Field.

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引用本文

易浩,郭挺,孙连忠.顺北油气田二叠系火成岩钻井技术研究与应用[J].钻探工程,2024,51(1):131-138.
YI Hao, GUO Ting, SUN Lianzhong. Study and application of drilling technology for Permian igneous rocks in Shunbei Oil and Gas Field[J]. Drilling Engineering, 2024,51(1):131-138.

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历史
  • 收稿日期:2023-07-02
  • 最后修改日期:2023-10-10
  • 录用日期:2023-11-06
  • 在线发布日期: 2024-01-26
  • 出版日期: 2024-01-10
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