雄安新区D19井破碎热储层气举反循环钻进技术
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1.山东省地质矿产勘查开发局第二水文地质工程地质大队(山东省鲁北地质工程勘察院),山东 德州 253072;2.山东省地热清洁能源探测开发与回灌工程技术研究中心,山东 德州 253072

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中图分类号:

P634;TE249

基金项目:

中国地质调查局地质调查项目“雄安地热清洁能源调查评价”(编号:DD20189112);山东省地质勘查引领示范与科技攻关项目“高温地热超深孔勘查取心钻探关键技术研究与应用”(编号:KY202219)


Gas lift reverse circulation drilling technology for D19 well in broken thermal reservoir in Xiong’an New Area
Author:
Affiliation:

1.The Second Hydrogeology and Engineering Geology Brigade of Shandong Provincial Bureau of Geological Survey (Lubei Geological Engineering Survey Institute of Shandong Province), Dezhou Shandong 253072, China;2.Shandong Geothermal Clean Energy Exploration and Development and Recharging Engineering Technology;Research Center, Dezhou Shandong 253072, China

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    摘要:

    D19井是雄安新区地热清洁能源调查评价项目的一个勘探孔,完钻井深4021.78 m,揭穿雾迷山组和高于庄组2个热储层。为应对热储层钻进严重漏失及保护热储层,选用了气举反循环钻进工艺。对深井气举反循环钻进设备进行配套,同时对双壁钻杆下深、风量等工艺参数进行了现场试验优选。针对钻遇复杂破碎地层时返水(渣)通道经常堵塞无法顺利钻进的问题,研制出了适宜于破碎地层气举反循环钻进的防堵进水接头,同时对进水(渣)口进行保护,有效地解决了破碎地层气举反循环钻进易堵塞的难题,顺利完成了钻探任务。完善了极破碎热储层气举反循环钻进工艺技术,为气举反循环钻进工艺在破碎热储层的应用和推广打下了基础。

    Abstract:

    Well D19 is an exploration hole in the geothermal clean energy survey and evaluation project in Xiong’an New Area. Drilling was completed at 4021.78m, penetrating two thermal reservoirs each in Wumishan Formation and Gaoyuzhuang Formation. Gas lift reverse circulation drilling was used to deal with serious leakage of the thermal reservoirs and protect the thermal reservoirs. The drilling equipment was selected, and the setting depth of the dual wall drilling string and the air volume were tested and optimized. In view of the drilling difficulty due to blockage in the return (cuttings) channel encountered in complex broken strata in the process of gas lift reverse circulation drilling, an anti-blocking inlet sub suitable for the reverse circulation drilling broken strata with protection of the inlet (cuttings) port have been developed. It effectively solved the blockage difficulty with gas lifting reverse circulation drilling in broken formation, and the drilling job was successfully completed. The gas lift reverse circulation drilling process for extremely broken thermal reservoir has been improved, which lays a foundation for the application and promotion of the gas lifting reverse cycle drilling process in broken thermal reservoirs.

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赵长亮,王勇军,聂德久,等.雄安新区D19井破碎热储层气举反循环钻进技术[J].钻探工程,2022,49(4):137-143.
ZHAO Changliang, WANG Yongjun, NIE Dejiu, et al. Gas lift reverse circulation drilling technology for D19 well in broken thermal reservoir in Xiong’an New Area[J]. Drilling Engineering, 2022,49(4):137-143.

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历史
  • 收稿日期:2022-02-11
  • 最后修改日期:2022-06-15
  • 录用日期:2022-06-17
  • 在线发布日期: 2022-07-18
  • 出版日期: 2022-07-10
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